Ford 7.3L Power Stroke (1999-2003) :: Manifold To Up-Pipe Bolts Seized
Apr 22, 2015
So I had recently developed a leak in the up pipes behind the collector. Big surprise, right?
Well, a 6-point socket was spinning on the collector bolts (probably from rust) so I decided to cut the manifold to up pipe bolts. Got the up pipes off/out. Well after and <acronym title="Manifold Absolute Pressure">MAP</acronym> gas torch, I can't punch ANY of the bolts out.
There is little to no room to get to the bolts. (I have the down pipe removed.) At this point I'll try a few more doses of hot wrench and PB Blaster, but if I have to do the manifolds I'll just pull the engine, since chances are there will be at least one stuck bolt there, too. I really don't want to go that, but eventually I'll need to install my new oil pan anyway.
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Just bought a 03, the seller showed me a exhaust leak. I found a bolt broken off, flush with the head. Looked at the passenger side when I got home, that side leaks too, and found one broken off bolt there too. Question, are these easy to do? As in, I have extracted broken bolts before, but they where on my V10 and I could just weld nuts to them and they came right out.
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I had a fuel starvation problem because Ford painted the inside of the fuel tank and the paint was coming off and clogging the filters and because I foolishly drove it I now have white smoke spewing out of the tail pipe and an engine miss.
I also explained that I thought that the white smoke did not smell sweet like antifreeze, but rather like diesel. (Hoping that a head gasket replacement is not required.)
I am in the middle of doing the Hutch Mod with frame-mounted Racor PS120-2 jar-type screen pre-pump filter and shortening my previous Harpoon Mod and paint stripping and powerwashing the inside of my tank. Next I plan to move on toward the engine issue.
This evening I was under the van with a flashlight and I noticed that there was a black liquid of some sort at the driver's side exhaust manifold where it joins the up-pipe. At first I was afraid to touch it fearing that it would be carbon-sooted water, but it felt and tasted like carbon-sooted diesel.
And since I haven't started the engine in two weeks and it has been routinely near or over 100F in Sacramento, water would have likely evaporated days ago.
Does it make sense if the fuel starvation problem caused an injector nozzle or its cup to crack or to stick open or to otherwise spew unburnt fuel into the exhaust manifold which would cause the white smoke? Obviously, the unburnt fuel must get from the affected cylinder(s) to the tail pipe somehow, which likely means out the exhaust valve, through the exhaust manifold to the up-pipe and through the turbo to the exhaust pipe and finally to the tail pipe.
See pictures at my CP. I can't figure out how to attach them or put them inline here because it still says I can't do attachments.
What is my next move? Remove the driver's side valve cover? If so, what should I look for, etc.?
2002 E350 extended body van 7.3 diesel auto trans converted to 4x4 (bought new)
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I just finished installing a new turbo (shaft play and lots of oil in the compressor side), RR up-pipes, and T500 (250k and once had a very long crank to get the ICP up to start).
Anyway, except for another exhaust leak at the pass side up-pipe to manifold, it seemed to run okay but with lots of white smoke. I only have about 50 miles after the install, when it suddenly starting surging and made a lot of loud knocking noises. This then went away and came back again rather quickly. I was close to home, so I made back under power. I also received the two codes listed. My IPR is original, but two summers ago I installed the IPR re-seal kit. Everything on the IPR looked good when it came off for the T500.
After reading around, I saw that low fuel pressure / air in fuel can cause problems. I connected a pressure gauge to the pre-filter port on the filter housing, and got 40psi at idle. I then took a diesel shower and blew out the fuel line into the tank. After re-connecting it, the fuel pressure stayed the same but the engines idles much better, but still has blue smoke. It's the original fuel pump (to me anyway) and original fuel line connections.
I have about 3/4 tank, and no place to put it, so I'd need to run it out for the Hutch mod, or least to get in there and inspect. Would eliminating the Ford connections at the pump be worthwhile for now, and is 40psi at idle adequate? Wondering if it's time for a fuel pump?
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I can't get my exhaust manifold bolts off. They are in bad shape. The 10mm is too loose and 3/8 just rounds. I have had the torches on them too! Can the bolts be cut off with a torch?? Haven't broken any. Can't get the bolt heads to move. It's an 04, original manifolds. I am working the driver's side. I can't figure this one out. How to get this manifold off?
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Would it be a good idea to change the injector hold down bolts when I do the injector o-rings? They have never been out at 333,000 miles.
Plan on doing glow plugs, injector wiring, valve cover gasket's, intercooler pipes and the dreaded oil cooler.
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Tried to flush it and got as far as draining everything. I can't hook up my T and begin the flushing process because I can't remove the thermostat. I have a buddy who can get the bolt out but I'd have to be able to drive the truck to him. I've tried just about everything to remove it. I did manage to find some replacements for when I do get the last one out though .Is there a way to still flush this thing like maybe just hook up the hose to the t and run the engine with the heat on to open the thermostat?
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I have been reading here about alternate methods to torquing the hold down bolts for the injectors. This winter I replaced my old stock split shots with new alliant single shots. I installed the injectors into a cold engine and torqued the hold down bolts to 10 ft lbs. I did not ever go back and re-tighten.
Is it suggested to go in and re-tighten the injector hold down bolts to 10 ft-lbs after the engine has been heated up and cooled down? What are some symptoms of a loose injector? I am imagining premature wear on the injector cups, low compression and maybe some mixing of oil into the combustion chamber.
Did just throw the injectors in and go back later to retorque only to find they were all fine or were some loose?
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Are we supposed to put anti sieze on the turbo to pedestal bolts. They were really hard to break loose when I pulled it Cheater bar tight. 18 ft. lbs sound right ?
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I would I have a 01 7.3 e350 with 111k miles. I drove the van a couple of days ago.it sat for 2 days and now it wont go past 30mph.the van shakes crazy and went when i hit the petal no power with smoke coming out the tail pipe sometimes. When I shut the van off and restart it to drive it,it sounds better. I changed the fuel filter with motorcraft and changed the oil. Here is the kicker. It ran good after I changed the fuel filter the whole day and now its 4th of july and I went to get some drinks and it happened again.
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I read 18lbs for the water pump but it took a cheater bar (perhaps due to corrosion) to get the water pump lower elbow bolts off.
On reinstallation, what should the lower elbow bolts be torqued to? Checked the sticky (Ziggy's Torque Specs) but didn't see the specs for this item.
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I wanted to know what happens when the injector hold down bolts are not torqued down to spec, what problems would arise and could it be a reason for somewhat hard starting?
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Small oil leak looks like coming down by drivers side up pipe. I don't think it's the turbo o rings. Better not be. But could be I guess. Anyways. It runs down somewhere by the up pipe down onto transmission. I'm not loosing tremendous oil or anything.
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I own a e1999 Ford F350 7.3 4x4 with a Garrett GTP38R turbo. I have been having issues with very little power and pulled an CEL of P0221. I know it's for the APS and have been trying to trouble shoot it as a new APS has not fixed the problem. However, while working on that I just noticed an oil leak appear. I tracked it down and can visibly see it leaking out the top of the passenger side exhaust manifold in two places. It is seeping out the top. Is oil supposed to even be running through here like that?
I recently replaced my up pipes with the newer style bellowed ones. While I had the turbo off I replaced all the o-rings top and bottom and did the EBPV delete on the pedestal. I have been having very little power and cannot the truck over 5-10 MPH and stays at low RPM's so I originally thought it was the leaky up pipes. Those were fixed along with fuel pressure checks which came back good. I then pulled the P0221 code finally. While I had the turbo off I inspected it and it did spin freely and had no side to side play in it.
What was unusual to me was there was a small pooling of oil in the turbo when I took it off. I know the CCV goes through here so some oil is normal. Also, when I was diagnosing the up pipe leak I could see a small amount of oil spraying out the blown donut gasket along with the exhaust gases. I don't think that is normal.
Is there an internal seal in the turbo that can go bad causing oil to spill into my exhaust and possibly leak at the exhaust manifold? Or do I have an internal oil leak from somewhere else?
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So I received my International bellowed up pipes from Riffraff and I figure I will start soaking all of the bolts with some aerokroil before I get started on monday and I see the very last bolt head near the up pipe is gone. The bolt is there but the head is gone and you can definitely see soot buildup everywhere near it. I don't know if I should order a new manifold for the passenger side and new bolts, order a driver and passenger side manifold and new bolts, or just order one set of new bolts and try to get take the passenger side manifold off and replace the one broken bolt.
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I managed to get the drivers side exhaust manifold and all of its bolts off no problem. On the passenger side I had 1 bolt head that was already broken and I have only 1 other that is still holding on for dear life. I've been soaking it in aerokroil for awhile now and no luck. I tried some PB blaster today because I am willing to try anything. I also tried heating up the bolt with a torch and some map gas but not sure if I am heating it up enough or not. Anyways, everything else has been going great, got the uppipes off and the valley, turbo and pedestal all cleaned up good. Just need to get the last whole bolt and broken bolt out so I can install the new manifolds. What I should try to remove the last 2 bolts. How hot should I get the bolt when trying to remove it? Or should I be heating the engine block?
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Well i had an exhaust leak on this F250 and so I started torquing the bolts on the manifold to the head. (45 ft.lbs) A couple were very loose so I was thinking "Great, this may fix my problem!"
My first mistake was probably the Harbor Freight Tools torque wrench.
I am on the driver side, second from the rear and then bang! I see a gaping hole where the bolt used to be. Bolt on the floor. I cant see up in the hole to the head, I think it broke flush with the head.
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I just came back from a 200 mile trip and parked my truck. Next day, got in the truck and turned the key.... it turned over and white smoke coming out the tail pipe. After doing some research(you tube),I ruled out cps sensor because it was showing low rpms on tach. Replaced glow plug relay and still have same issue.. what else to look at that I can do without getting it towed. Hunting season coming soon and I need the beast.
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I recently installed a Banks Ram Air Intake on my stock 1999.5 powerstroke and wow did it ever wake up the turbo. A few weeks later i installed a Flo-Pro 5" stainless exhaust from turbo back with no muffler. The truck is running better than it has in years and with 272000 miles, I am pleased with the results. HOWEVER, I have since noticed a little black sticky soot coming out of the tail pipe, a bit of vapor (no oil spitting) from the oil filler tube with the lid off, and now my dip stick tube where it enters the oil pan is leaking. What is going on , or am I now chasing and fixing week points on this truck?
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Ok I'm working on a 2000 7.3 on a F550 truck was running but had no power so we changed out all the injectors and glow plugs and rebuilt the turbo now there is no start it turns over and were getting black smoke from the tail pipe. What is going on with it?
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I have a 97 f350 crew cab xl stock everything. 351 windsor in it I do believe. as of right now He is broken down pulled apart in my garage. Due to a much requested headgasket replacement. In any event long story short I got him all apart to discover that there was someone in it before me & had broken the infamous exhaust manifold bolts (5) and two of the lower intake bolts, (of course I've tried the correct route in removing these broken bolts/studs but again the year of the truck (1997) & its bone stock no way their moving...
So of course I tried the next best thing (on a budget) which is to drill them out, but I went to far into the exhaust manifold bolt holes, And now I believe that I've ruined the heads is this so? If so who knows where i can get a decent set of bolt on heads ready to go. yes this is my daily driver & since He's been down I've been going deeper in dept.
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